Re: Intro from Prescott
Posted: Wed Jun 09, 2021 9:21 am
Hi Y'all
Reviving this as I finally got to tinkering this last week or so. To refresh the back story, I had mistakenly put a gallon fresh gas in the tank about a year ago and forgot about the old outdated gas in the return line so soon had polluted the system and stuck the grose jet fuel bowl valves. In taking the float bowl tops off I managed to bend up the floats so had messed up where Z Therapy had set them. Now I know the rotate until they can come off method. I did fill the dampers with the suggested ATF and rechecked that. Then made sure the suction pistons were free - both were stuck a little.
To prep I pulled the plugs and squirted in some 0W16 synthetic and let it soak a day then bumped the starter several times and added more oil and let it sit again, then ran the starter for longer. Then got a gallon of fresh gas and pulled the tank line and hooked up a long hose to the gas can and hooked up the sight glasses to both bowls and blocked off the rear fuel line so as to only run the front carb. It immediately filled the bowl and started leaking out everywhere! SO after cleaning up the mess and straightening out the float and tweaking the actuator tab I had a 1/4" or less in the glass tube so redid it again and got a good level.
Then I got to doing the rear carb and after a bit noticed that the gas was dripping out of the throttle body and was all the way up the sight glass! So I disconnected the inlet fuel hose and stuck some paper towel in the carb throat and finished the rear carb. Figuring that the grose jet had leftover crud from the bad gas of a year ago pulled the front apart and pulled the grose jet and let it soak in gas a day. It did better so it was time for a test fire. A little choke and hit it and she started right up! A very lumpy idle and the front carb fuel bowl level climbed very high and the rear came up to about an inch. I think that the extra pressure from the stock fuel pump might have been the cause.
So I readjusted the tabs again the next day and tried it out again. That front still has too high of a level so I think the grose jet may be a goner? Bummer as they seem to no longer be in production. Is there any better thing to soak them in? Carb cleaner spray?
Also of concern is that while it stayed running until the choke could come off, the idle was lumpy as heck and any throttle was killing it. After releasing the throttle it would idle a hair faster a second or two but just as lumpy. Adjusting the mixture knobs on the bottom and idle screws did nothing. Next up is to pull the plugs. I'm betting they are wet! Think I should get some new ones?
I should mention that it ran fine before I took it all apart to send in the carbs to Z Therapy. I did pull the stock exhaust manifold and installed the MSA 6 into one header and that there seems to be no exhaust leaks and also had a new 2" exhaust run with a turbo muffler at the back end.
I'd sure appreciate any ideas on what to check or on what may be the issue. Many thanks in advance!!!
Reviving this as I finally got to tinkering this last week or so. To refresh the back story, I had mistakenly put a gallon fresh gas in the tank about a year ago and forgot about the old outdated gas in the return line so soon had polluted the system and stuck the grose jet fuel bowl valves. In taking the float bowl tops off I managed to bend up the floats so had messed up where Z Therapy had set them. Now I know the rotate until they can come off method. I did fill the dampers with the suggested ATF and rechecked that. Then made sure the suction pistons were free - both were stuck a little.
To prep I pulled the plugs and squirted in some 0W16 synthetic and let it soak a day then bumped the starter several times and added more oil and let it sit again, then ran the starter for longer. Then got a gallon of fresh gas and pulled the tank line and hooked up a long hose to the gas can and hooked up the sight glasses to both bowls and blocked off the rear fuel line so as to only run the front carb. It immediately filled the bowl and started leaking out everywhere! SO after cleaning up the mess and straightening out the float and tweaking the actuator tab I had a 1/4" or less in the glass tube so redid it again and got a good level.
Then I got to doing the rear carb and after a bit noticed that the gas was dripping out of the throttle body and was all the way up the sight glass! So I disconnected the inlet fuel hose and stuck some paper towel in the carb throat and finished the rear carb. Figuring that the grose jet had leftover crud from the bad gas of a year ago pulled the front apart and pulled the grose jet and let it soak in gas a day. It did better so it was time for a test fire. A little choke and hit it and she started right up! A very lumpy idle and the front carb fuel bowl level climbed very high and the rear came up to about an inch. I think that the extra pressure from the stock fuel pump might have been the cause.
So I readjusted the tabs again the next day and tried it out again. That front still has too high of a level so I think the grose jet may be a goner? Bummer as they seem to no longer be in production. Is there any better thing to soak them in? Carb cleaner spray?
Also of concern is that while it stayed running until the choke could come off, the idle was lumpy as heck and any throttle was killing it. After releasing the throttle it would idle a hair faster a second or two but just as lumpy. Adjusting the mixture knobs on the bottom and idle screws did nothing. Next up is to pull the plugs. I'm betting they are wet! Think I should get some new ones?
I should mention that it ran fine before I took it all apart to send in the carbs to Z Therapy. I did pull the stock exhaust manifold and installed the MSA 6 into one header and that there seems to be no exhaust leaks and also had a new 2" exhaust run with a turbo muffler at the back end.
I'd sure appreciate any ideas on what to check or on what may be the issue. Many thanks in advance!!!